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fbh31118

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Everything posted by fbh31118

  1. LOL. No it's not. My handle is my mothers 1940 H at there farm. Had to memorize it to gets parts one day and thought it would make a cool handle, 20 plus years ago. The H in the picture is a 1943 Mine is slopped out enough that I need to do something but just trying to decide what I want to do with it. I was curious what was on the inside but wanted to keep as much of it original as I can. Not really worth the extra work but not awful either. This one has the grease zerk in one end as well but I couldnt find the picture of it.
  2. Anyone had this joint apart before? I'm considering tearing this apart and repairing.
  3. David Kirk has an entire write up on these engines and the mechanics behind it. I know that there are some who don't agree and others who are convinced. This crank was not individually balanced by anyone. I will report back good or bad. Guess I've done dumber things. 😆
  4. Crank has returned with Kirk Engine balance plate installed! Fun times ahead.
  5. Great news! Nothing better than seeing the Ol Axial Flow combine in the field.
  6. A few from the early days Our oldest Kathleen on the left. Seems like one of the girls was Art A's daughter but not sure about the other.
  7. Yes, she's a senior in high school this year! Doesn't seem possible.
  8. I will say that I have never had this engine apart before so I have no way of speaking to the condition of the parts that went into the engine or the level of attention that may or may not have gone into it. 😉 I have put an exhaust valve and a head gasket on it in years passed to I will pay special attention to the carb when I put it back together. I plan on putting a balance plate in it and ball honing the cylinder with a stock set of rings and piston. I also hope to recut the valve seats and have the valves ground if I can find someone to do them. This is a thumping little engine and I love it! It runs out of traction way before it runs out of power for us. Can't wait to have this back together!
  9. Good news! Rod journal and bore are in spec for standard parts.
  10. Block is empty and the components cleaned up. Guessing it has a Kohler piston but the rod is anyone's guess. At the minimum it's looking like valve seats need to be recut, valves ground, piston, rings and possible .10 over bore. Wrist pin and rod journal looked really good by eye. Waiting to get some tools to measure the parts up and see what we've got.
  11. Nice! I'm hoping I got all of ours taken care of on this go around.
  12. That's my plan. Hoping I can get the 122 back together this month. Lots of oil burning........
  13. It really does, had it apart 3 times to get it right though. Several things I would do differently after getting all the way through it now.
  14. Got the engine torn down this weekend. It was surprising how good the crank journal and con rod looked. The piston skirts were a little rough looking and possibly the source of the oil blow by but will have to measure to know what's going on. There is zero ridge in this block so I'm leaning towards a possible valve guide issues or the cylinder out of round. I'm also wondering if I should even bother replacing the main bearings. Here's a look at a few pictures I took this weekend.
  15. A little update video. Great running little engine.
  16. This is the seal that failed in Tammies tractor the first time we put a plow on it. I set the plow up and she made one pass before it blew out on the headland.😁😆
  17. Got the wifes 782 our for a bath that it needed desperately and pulled the motor. There is a leak coming from some where, so the block was caked with dirt pretty bad. Also, fuel pump diaphram was failing and leaking into the block so a new fuel pump went in. Started with removing the tin and repaired the starter, which had gotten loose, with a few washers and lock nuts. Got a roll of gasket paper and cut out some new gaskets for the valve covers, which is where I hope the leaks were coming from. Hoping to get the oil changed today and give it a test start to see what happens. We went completely through this motor many years ago as our first 'learning' experience with engine rebuilding. Pretty sure I had this motor apart 3 times to get is close to being right.😉😆 The plus side was taking the plugs out of the engine yesterday and seeing that they were completely clean. It appears to have been running well other than the external oil leak and fuel pump failure. I know, I should go electric on the pump but the mechanical has worked so well for so long. One of the tires has a bad valve stem, which will be headed to the tire shop for a new stem and reload of beat juice, now that I think about it........ Hope to have it up and running with fresh fluids this next weekend. The hydro fluid hasn't been changed in years but honestly it might have 20 hours on it at the most. I haven't bought filters for the hydro in forever, hope Cub still makes them.😁
  18. Good point, I had forgotten about MidWest Super Cub. I'm really interested in the crank balancing and deleting the balance gears. It's really been a solid motor the whole time we have run it but it's going through a lot of oil.
  19. Stock size on the front and back.
  20. fbh31118

    Crap!

    I so need to do this repair on my wifes 782. The parts are getting worn pretty bad.
  21. The time to get the Cubs out has finally arrived!!! Our 122 has a very special story and is very important to our family and as such is going to be the next in line for a little tlc. We plan on pulling the engine and tear it down to get measured up and get a rebuild started. I would love to do a David Kirk style project but I'm not sure if the parts are even out there let alone for a standard rebuild. What have you seen out there these days?
  22. Hey Plow, can I bring the H and the #8? 😁😆😉 J/K
  23. I feel your pain be it on a much smaller scale. I have gone rounds with electrical rebuilds with my H project and still trying to eliminate them. It's very frustrating to know enough to identify the problem but not have the equipment or experience to make the proper repair. My original rebuilder went through my 3 brush generator and sent it back with a regulator instead of a cutout relay. That was after explaining in person and on the telephone what I was expecting. Disappointing to say the least. Good luck Tony! I know you'll get to the bottom of the problem one way or another.
  24. I would be interested to see that as well. Can't say that I've ever seen one that had them.
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